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MACONDO BLOWOUT

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MACONDO BLOWOUT

  1. 1. MACONDO BLOWOUT: THE ACCIDENT AND THE FAILURE PATH
  2. 2. Scheme of the Well – Final Mechanical State
  3. 3. Sequence of Operations
  4. 4. Operational details of the cementation of the combined casing of 7” x 9-5/8”
  5. 5. Sequence of Operations
  6. 6. Details Negative Pressure Test or Influx Test (Unbalance Test)
  7. 7. Negative Pressure Test (Unbalance Test)
  8. 8. Details of the erroneous validation to the “negative pressure”
  9. 9. Identification of Immediate Causes for uncontrolled well flow Well integrity was not established or failed • 1 Annulus cement barrier did not isolate hydrocarbons • 2 Shoe track barriers did not isolate hydrocarbons Hydrocarbons entered the well undetected and well control was lost • 3 Negative pressure test was accepted although well integrity had not been established • 4 Influx was not recognized until hydrocarbons were in riser • 5 Well control response actions failed to regain control of well Hydrocarbons ignited on the Deepwater Horizon • 6 Diversion to mud gas separator resulted in gas venting onto rig • 7 Fire and gas system did not prevent hydrocarbon Ignition Blowout preventer did not seal the well • 8 Blowout preventer (BOP) emergency modes did not • 9 seal well
  10. 10. Failures in the Emergency Functions to Secure the Well
  11. 11. Actions applied to seal the well stop uncontrolled flow

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